Avocado Maytag KA606 / KDG606 Parts Machine Pair

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A peek inside the water pump. My phone shot isn't great, but I'm not sure there are any fins (vanes?) that were not damaged. A number of them were missing entirely. So this wasn't pumping nearly as well as it should have been.

This pump is old enough to be of the split type, so I'll pull the cover and look inside later just for grins.

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Motor, pump, and transmission pulley removed. It's interesting to me that Maytag gave the half-moon cutout so the water pump could be removed without removing the pulley, yet required the pulley removal for the motor? The set screw on the motor pulley took a 2' cheater pipe on my Allen wrench - I thought it was going to snap, but it came free...

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Then from here is where things went sideways. After removing the lock bolt and clip, I was able to hammer (with great effort) the brake package removal tool enough to get it to turn. But the brake just wouldn't come free from the transmission. Persuasion from the sides didn't work either - it moved, but wouldn't come free.

So I grabbed my large puller, and put some gentle pressure on it while I tapped around with the hammer. This is NOT a good way to do this, so there is a chance my nylon gear in the transmission is now damaged. I'll find out once I have it apart.

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... and here is why it was stuck. The large bearing is just completely destroyed. It was rusted/seized to the brake, the inner race seized to the transmission housing, and what was left of the cage was a mangled mess rattling around inside and the balls free to go wherever they pleased. The edge of the outer race had flared, leaving a large sharp edge on the bottom. This must have sounded horrible during spins!

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Out came the puller again to remove the inner bearing race. This was too far of a reach for my small puller, and the large puller barely grabbed the lip of the race, but it worked.

The socket over the input shaft is what I should have done the prior time I used the puller. I don't know why I didn't think of it at the time...

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Maytag washer, disassembly or demolition?

Wow, Dave, fun to take something apart that’s in such bad shape but you’re not going to yield very many useful parts and when you consider how plentiful Maytag washers are not sure, it’s worth the effort but fun.

That washer definitely had some water sitting in it for a couple of years. If there was ever a washer that should be turned into a new Kia. This was probably it lol

But it’s need to see something difficult taken apart. Thanks for posting all the great pictures

John.
 
Oh my goodness. Dave, this is by far one of the worst outer tubs I've ever seen. But holy cow, look at that bearing! Let's hope that the damper is in good enough shape to make all of this effort worth the while.

Ben
 
Reply number 37

If the Maytag washer just squeals, as the tub comes to a stop, it’s not the belts you have a dry brake assembly.

Usually adding an ounce or two of oil will solve the problem even though the brake lighting might be worn away, that will usually make it work for many years, this condition does not hurt anything if you want to keep using it and it’s kind of a nice signal the first time at screeches go put fabric softener in the second time you take the clothes out and put them in the dryer.

John.
 
Thanks guys. I've been trying to figure it out - do you think the damaged water pump, perhaps much earlier in its life, might have been a contributor to its demise? I'm wondering if the machine became incapable of fully pumping out the water, basically leaving water (and detergent and debris) in the tub every time it ran... ?

These machines don't owe me anything - I got my money's worth just from the two-speed motors. And they aren't sentimental, and no laundry is piling up waiting for them to be fixed, so that all makes the teardown more enjoyable. So it's just practice for the future, and basically anything salvageable is a bonus.

I *do* now have a better understanding why service technicians will no longer work on these. Even if a customer was OK with the labor time, there's just no telling what you will find inside, or how many parts you will ultimately need to replace... [this post was last edited: 12/6/2022-10:17]
 
A few more pictures - the spin tube has some heavy scoring on it, so it's been running dry for a while. A lot of crud buildup too, both of which are mirrored on the inside of the outer bushing as well. The agitator shaft isn't the worst I've seen, but I'll have to wire brush it to see what is crud and what is rust. I don't remember feeling any lateral play in the top bushing.

I have no plans to rebuild this transmission anytime soon, if ever, but I might split the case at some point just in the name of discovery. Either way, I'll hold onto it in case I need an internal part in the future (such as the gear that shattered its teeth in my parents A308).
https://www.automaticwasher.org/cgi-bin/TD/TD-VIEWTHREAD.cgi?76329_22~1
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Here is what remained of the upper seal on the agitator shaft. The rubber and the spring were both destroyed. (They were like this inside the stem - the spring was in pieces before it was removed.)

That half-missing flat washer in the upper left corner of the photo - does anyone recognize that? I found it on the floor when I was cleaning up, and have no idea where on the machine it came from?

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Here's the base plate. I haven't cleaned it at all in this picture, so at least some of what looks like rust is lint/detergent/debris buildup. I'll keep this for sure for future projects - likely swapping it and a two-speed motor into the A408 when I do the eventual A806 conversion.

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Close up of the damper pads. The prior owner mentioned replacing these, but I'm not sure how long ago that was done. There is a section where the pad is missing (or perhaps just a gap from where they were installed), but it looks like the surrounding pads were thick enough to compensate - I don't see any evidence that the metal in this section had rubbed?

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The half missing washer is the remains of one of the leaded washers for the three outer tub supports. Not surprised to see it in such poor shape.

Seeing the remains of the agitator shaft seal is yet another reminder for anyone putting one of these in service from the wild to check and replace this seal immediately, including all Maytag wringers. Many of these are well over 50 years old now and most will look and will crumble like this one.

Ben
 
Close-up of the damper itself. I don't see or feel any damage to it - nothing is rough, nothing particularly shiny, and no difference in the profile as you follow it around. The dark spots are bits of the damper pad material, glue, or something else stuck to the surface that I'll need to clean off. Is there anything else I should look for?

The rusty debris from the large bearing will need to be cleaned out. My understanding is that the outer edge of that bearing is captured/located by the brake assembly - and this damper only needs to press on the edge of the outer race to lock it in place, correct?

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So it's been a while, but we tore into the KDG606 dryer this week...

It had clearly been in the process of being worked on, but it's tough to say what spurred the repair attempt, or (like the washer), which fault took the machine out of service.

Both belts were off, and the idler pulley was on the shaft, but installed backwards, and the sliding mount was jammed in place. The belts were in very poor shape, with large chunks hanging off.

The brush holder and carbon brush were missing, with the wire lug from the drum paddles just hanging loose. No fresh wear on the slip rings, so this might have been disabled some time ago, but I'm not sure how the dryer could have been used in this state?

There were two felt strips loose in the bottom of the machine - one a thin one (about an inch wide?), and then the thicker felt that goes around the outside of the halo, which was still partially attached, but otherwise also bunched up at the bottom of the machine.

I was surprised how much corrosion damage there was inside the dryer. The crimped on electrical connectors just snapped when attempting to remove them.

Mechanically, it seemed fine. The drum spun OK, as did the motor and the blower. The drum and blower bushings/shafts were completely dry after disassembly, so it hadn't seen oil in quite a while, but still spun fine. Very little rust on the base at all, other than the light internal corrosion.

The dial was missing the plastic piece which creates the detents, so the knob position is just free spin, but otherwise seemed to be complete and could be operated. The cycle end solenoid would take some cleaning to make it move freely.

Lots of lint and debris, but a 1976 nickel was the most interesting thing found in the base or bottom of the halo. (Anyone know why the nickel didn't get a bicentennial version?)
 
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