Hi folks. I am new here to this forum, but have been online on other places for quite some time.
A Facebook friend suggested that I share this project here. I have tried several times to make a new thread but have as of yet been unsuccessful. Furthermore, it is telling me I can not post again for 30 minutes after each post because I am a "new member."
Anyway - the Frigidaire! I was working at a jobsite in southern Louisiana noticed an ad for an "antique refrigerator - not working." I envisioned a 1950's era fridge, such as one of the rounded Frigidaire Meter-Miser units. When I got there, it was a 1931 belt-drive Frigidaire! The compressor skid was missing, but the enamel cabinet was in OK shape, and all the trim was present and in excellent shape.
I discussed it with a fellow enthusiast who had acquired a very deteriorated, similar fridge which had its compressor in place. The rest of it was unsalvageable, however.
I was able to get the compressor skid, along with a few other spare mechanical parts for the fridge.
This refrigerator is unlike anything I have worked on before. It is a vapor compression system, but that is where the similarities with modern units end.
The compressor is driven by a fan belt, with a large Delco electric motor. All the electrics on it are Delco-Remy. The same Delco-Remy who makes the electrics for our old GM cars!
The shaft seal shredded when I turned the compressor flywheel by hand. A small amount of sulphur dioxide (SO2) pressure was still in the system, which escaped at that time. This was a good finding, because the pressure kept moisture from going in and reacting with the SO2 and corroding the compressor beyond repair.
I constructed a new shaft seal assembly by turning down the front part of the housing from a modern GM car A/C compressor and installing a new seal in this part. The compressor was otherwise in excellent shape inside.
The evaporator is where it gets weird. There is a float valve inside the evaporator header. It allows liquid refrigerant to flow into the evaporator and then stops the flow when the evaporator is full of liquid. This low-side float system was not used often or for very long.
When I finally got the cabinet home from Louisiana, I started investigating the condition and found the insulation was bad. It was unlike anything I had seen before. The panels of insulation were made of wooden frames, with layers of aluminum foil and paper inside. This created air spaces to give an insulation effect. Due to the advanced deterioration of this, I replaced it with Styrofoam, sealed in place with expanding foam sealant.
The float valve and control were the only parts requiring adjustments for the different pressure and density of the R152A refrigerant. After this was taken care of, it cooled down to 0 degrees without a door gasket even installed at all. Now that the door gasket is new, it runs at about a 20% run time. That's with a 30 degree cabinet temp in a 90 degree barn, in Alabama.
I started making videos of it as soon as I found it. I have posted them on YouTube with links at the end of each segment for the next one. Here is the first segment:
Also, the rebuild has been fully documented on another forum, in this thread:
http://monitortop.freeforums.net/thread/1370
I hope you guys have found this interesting. I refused to believe the general consensus that these can not be fixed and made to work again. Heck, it worked when it was new. It is a purely mechanical system, so if all the mechanical parts work properly it can't NOT work!
NOTE: I want to share more photos, but there is a 20 limit. Will have to post later with more.
Sincerely,
David




















A Facebook friend suggested that I share this project here. I have tried several times to make a new thread but have as of yet been unsuccessful. Furthermore, it is telling me I can not post again for 30 minutes after each post because I am a "new member."
Anyway - the Frigidaire! I was working at a jobsite in southern Louisiana noticed an ad for an "antique refrigerator - not working." I envisioned a 1950's era fridge, such as one of the rounded Frigidaire Meter-Miser units. When I got there, it was a 1931 belt-drive Frigidaire! The compressor skid was missing, but the enamel cabinet was in OK shape, and all the trim was present and in excellent shape.
I discussed it with a fellow enthusiast who had acquired a very deteriorated, similar fridge which had its compressor in place. The rest of it was unsalvageable, however.
I was able to get the compressor skid, along with a few other spare mechanical parts for the fridge.
This refrigerator is unlike anything I have worked on before. It is a vapor compression system, but that is where the similarities with modern units end.
The compressor is driven by a fan belt, with a large Delco electric motor. All the electrics on it are Delco-Remy. The same Delco-Remy who makes the electrics for our old GM cars!
The shaft seal shredded when I turned the compressor flywheel by hand. A small amount of sulphur dioxide (SO2) pressure was still in the system, which escaped at that time. This was a good finding, because the pressure kept moisture from going in and reacting with the SO2 and corroding the compressor beyond repair.
I constructed a new shaft seal assembly by turning down the front part of the housing from a modern GM car A/C compressor and installing a new seal in this part. The compressor was otherwise in excellent shape inside.
The evaporator is where it gets weird. There is a float valve inside the evaporator header. It allows liquid refrigerant to flow into the evaporator and then stops the flow when the evaporator is full of liquid. This low-side float system was not used often or for very long.
When I finally got the cabinet home from Louisiana, I started investigating the condition and found the insulation was bad. It was unlike anything I had seen before. The panels of insulation were made of wooden frames, with layers of aluminum foil and paper inside. This created air spaces to give an insulation effect. Due to the advanced deterioration of this, I replaced it with Styrofoam, sealed in place with expanding foam sealant.
The float valve and control were the only parts requiring adjustments for the different pressure and density of the R152A refrigerant. After this was taken care of, it cooled down to 0 degrees without a door gasket even installed at all. Now that the door gasket is new, it runs at about a 20% run time. That's with a 30 degree cabinet temp in a 90 degree barn, in Alabama.
I started making videos of it as soon as I found it. I have posted them on YouTube with links at the end of each segment for the next one. Here is the first segment:
Also, the rebuild has been fully documented on another forum, in this thread:
http://monitortop.freeforums.net/thread/1370
I hope you guys have found this interesting. I refused to believe the general consensus that these can not be fixed and made to work again. Heck, it worked when it was new. It is a purely mechanical system, so if all the mechanical parts work properly it can't NOT work!

NOTE: I want to share more photos, but there is a 20 limit. Will have to post later with more.
Sincerely,
David



















