The good news - we didn't pound the bearings out along with the drive tube.
Having a fresh pair of eyes helped here - Phil noted the scarring on the upper section of the tube.
I did not document the re-bearing process of this washer when I did it, so I cannot be sure that the tube was not already scarred or discoloured when I re-installed it.
But what really caught Phil's eye was the 'ring o rust' on the center post. Funnily enough, it looks like it is about the same height as the discolouration on the basket drive tube... I am going to guess that this is where the sticking occured causing the lack of spin. However, I recall that the Inglis tube had a dark spot on it at about the same height.
So, I have to wonder why this happened. Is it possible there is some sort of a leak in the center post that got into the bearing and the drive tube? I'm going to give it a good cleaning tomorrow and I have some POR15 if needed.
Now the $64,000 question - is the bearing still OK? I will guess that I did not lubricate it properly... Also, I am thinking I should replace the basket drive tube - or can I just clean up the old one?
At least I know the LK can be repaired now. And I am starting to miss having at least 1 working washer in St-Lib.... LOL
